In Nov 21 I relegated my Rail to second bike status after I bought a Kenevo SL.
In March 22 I decided to try and sell it as I needed the space in the garage. Unfortunately, when I took it out to clean it up for pics I realised that the motor wasn't working; it powered up and walk mode worked but pedalling did nothing. As it was out of warranty I got in touch with @Bearing Man and arranged a strip down and repair estimate.
This was the response;
And here's the pics he sent me...
The repair was completed in quick order and the motor has performed flawlessly ever since. I think the cost of repair was fair for the amount of work involved and the turnaround was very fast.
My apologies to @Bearing Man for not posting this sooner, but procrastination is my middle name....
In March 22 I decided to try and sell it as I needed the space in the garage. Unfortunately, when I took it out to clean it up for pics I realised that the motor wasn't working; it powered up and walk mode worked but pedalling did nothing. As it was out of warranty I got in touch with @Bearing Man and arranged a strip down and repair estimate.
This was the response;
And the quote for repair;Water/dirt has got in through the left hand crankshaft bearing which is what typically happens with the Gen4 motor we have found. The crankshaft assembly was semi -seized together as was the left hand crankshaft bearing. Please find attached estimate to repair, if you are happy to proceed just let us know and we will get your motor repaired as soon as possible.
And here's the pics he sent me...
The repair was completed in quick order and the motor has performed flawlessly ever since. I think the cost of repair was fair for the amount of work involved and the turnaround was very fast.
My apologies to @Bearing Man for not posting this sooner, but procrastination is my middle name....